Skip to main content
Skip to content
Case File
efta-02024511DOJ Data Set 10Other

EFTA02024511

Date
Unknown
Source
DOJ Data Set 10
Reference
efta-02024511
Pages
3
Persons
0
Integrity

Summary

Ask AI About This Document

0Share
PostReddit

Extracted Text (OCR)

EFTA Disclosure
Text extracted via OCR from the original document. May contain errors from the scanning process.
To: jeevacationftmail.comfjeevacation©gmail.comi; J Epstein[jeevacation©gmail.com] From: Zorro Ranch Sent Tue 8/21/2012 2:40:26 PM Subject: Fwd: Drilling Update FYI Sent from my iPhonc Begin forwarded message: From: Casey Cook Date: August 21, 2012 8:38:22 AM MDT To: Zorro Ranch Subject: Re: Fwd: Drilling Update Brice, As we discussed, the drillers were not confident of stability on first hole to stand up to an air operation, particularly the top 100 ft alluvium. So far, this new hole appears more stable, including top 100 ft. The first hole is still open, so airlift can be attempted, but hole collapse could be a problem. Please call with any questions. Casey C. On Aug 21, 2012 8:20 AM, "Zorro Ranch" wrote: FYI Sent from my iPhone Begin forwarded message: From: Jeffrey Epstein <jeevacation(Wgmail.com> Date: August 21, 2012 8:07:48 AM MDT To: Zorro Ranch Subject: Re: Drilling Update why did w not do this on the first well? this is not good news . EFTA_R1_00531446 EFTA02024511 On Tue, Aug 21, 2012 at 10:06 AM, Zorro Ranch wrote: Will get cost for compressor Recommend going to 800 and Then do air lift to get a basic idea of yield This is drillers approach as well Sent from my iPhone Begin forwarded message: From: Casey Cook Date: August 20, 2012 6:56:29 PM MDT To: bricc gordon Subject: Drilling Update Brice G.; As we discussed, the drill crew reached 640 ft in the exploratory borehole tonight with no observations of significant fluid loss. The driller has indicated he may be able to switch to an airlift operation without damaging the borehole, which will allow a preview of the how much water is coming from the hole. The operation will require an additional compressor that will add to the drilling cost, but it may be the only way to see how much water this hole can produce. With your approval, I will direct the drillers to set up for an air operation. I have a call into Ronnie Dennison at HGS to discuss the logistics and schedule for making the transition to air. I will let you know what he says. Please call to discuss any of this. Casey W. Cook, P.E. Balleau Groundwater, Inc. 901 Rio Grande Blvd. NW Suite F-242 Albuquerque, NM 87104 www. a eau.com EFTA_R1_00531447 EFTA02024512 *********************************************************** The information contained in this communication is confidential, may be attorney-client privileged, may constitute inside information, and is intended only for the use of the addressee. It is the property of Jeffrey Epstein Unauthorized use, disclosure or copying of this communication or any part thereof is strictly prohibited and may be unlawful. If you have received this communication in error, please notify us immediately by return c-mail or by e-mail to [email protected], and destroy this communication and all copies thereof, including all attachments. copyright -all rights reserved EFTA_R1_00531448 EFTA02024513

Technical Artifacts (3)

View in Artifacts Browser

Email addresses, URLs, phone numbers, and other technical indicators extracted from this document.

Domaineau.com
Domainwgmail.com

Forum Discussions

This document was digitized, indexed, and cross-referenced with 1,400+ persons in the Epstein files. 100% free, ad-free, and independent.

Annotations powered by Hypothesis. Select any text on this page to annotate or highlight it.