Case File
efta-efta00802479DOJ Data Set 9OtherAircraft Records & Condition Survey
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DOJ Data Set 9
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Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Gt ilfst n lams
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1
While complying with GIV CMP 330007 E-light ops test found aft battery E-light
annunciation 'OFF' would remain on when system active.
-CND, operating normal at this time-
2
While Complying with GIV cockpit avionics ramp check found cabin and galley 'OFF'
lights do not illuminate.
3 TBD, A/C has LED upgrade so may not be bulbs-
3
While Complying with GIV ramp check found copilot's aft ped. Panel lights imp.
Est 4 hr parts TBD
4
While Complying with GIV ramp check found pilot's and copilot's side console flood
lights inop.
Est 3 hr parts $2700 if bulbs
5
While Complying with GIV ramp check found Aircell phone system intercom feature not
working.
Est 4 hr parts TBD, cabinet handset will not power up and will need to be fixed first.
6
While Complying with avionics ramp check unable to locate security system control
unit.
7
While Complying with avionics ramp check found copilots audio control panel back
lighting imp.
Est 7 hr, $4000 if ACP, would recommend sending customers unit out for repair, it is
not standard ACP
8
While Complying with avionics inventory found #4 E-battery overload light flashing.
Est 4 hr, parts $4900 if battery
9
While Complying with avionics ramp check found #2 transponder not reporting mode S
information.
Est 10 hr, parts $12,700 if transponder
10
While Complying with avionics ramp check found both NAV rcvr's self-test inhibited.
Est 4 hr, parts TBD
11
While Complying with avionics ramp check found ELT flashed five times after system
was deactivated.
Est 2 hr, may not have NAV interface unit.
12
While Complying with avionics ramp check could not enter system maintenance test
mode.
Est 5 hr, parts TBD
13
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted loose/working rivet on floor on APU enclosure, below exhaust duct, approx 12"
aft of fwd wall and 3" inbd of Ext 107-APU-1 panel.
Est. 1 hr
Report Date: << DRAFT as of xx./xxJxxxx >>
Page 1 of x
EFTA00802479
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
( 111 11 fst n iris
•••••InIal
.1”i Name....
4 alA40Afre
Disc,
/4/prays'
Service Discrepancy
14
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted cracked stringer structure between access panels 106-APU-2 and 106-APU-3.
Est. 8 hr, $1200 parts
15
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted approx gap greater than 1/8" (oil canning) around enclosure Inbd floorboard
access panel below APU alternator.
Est. lhr
16
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted missing faying fire retardant sealant on access panels 106-APU-2, -3, and -4.
Est. 2hr $150 parts
17
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted lower plenum drain line chafed.
Est. 2 hr
18
While complying with GIV CMP 490053 APU Enclosure GTCP 36-150(G) - Inspection
noted missing fire retardant sealant from multiple areas of APU enclosure walls, ceiling
panels, stiffeners and brackets.
-Info only, no action necessary-
19
While complying with GIV CMP 553005 - Vertical Stabilizer / Rudder (External) -
Inspection noted Tail Strobe lens cracked
Est 2 hr, $1100 parts
20
While complying with GIV CMP 553005 - Vertical Stabilizer / Rudder (External) -
Inspection noted lower aft screw on access panel 109-RH TE-7 making contact with
rudder.
Est 4 hr
21
While complying with GIV CMP 551019 - Horizontal Stabilizer / Elevator (Exterior) (Left)
- Inspection noted horizontal stab rub block clearance beyond limits. Actual .032" Max
Allowable .025".
Est 8 hr, $50 parts
22
While complying with GIV CMP 553005 Vertical Stabilizer / Rudder (External) -
Inspection noted sheared rivet on Right lower side of RAM Air Inlet.
Est 2 hr
23
While complying with GIV CMP 553005 Vertical Stabilizer / Rudder (External) -
Inspection noted corrosion around drain hole on Left side of Upper Tail Cone.
Est 3 hr
24
While complying with GIV CMP 553005 Vertical Stabilizer / Rudder (External) -
Inspection noted APU door not fully closing.
Est 8 hr
25
While complying with GIV CMP 533005 Exterior Fuselage - Inspection noted Left Pitot
to have deformed tip
-Info only, deformation within allowable limits-
26
While complying with GIV CMP 533005 Exterior Fuselage - Inspection found Pilot Side
Window to have detached Aft Upper Terminal block.
Est 6 hrs
Report Date: << DRAFT as of xx/xxixxxx >>
Page 2 of x
EFTA00802480
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Gt 11 fst la tits
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27
While Compl
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Inspection foun
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that will require further evaluation.
Est 8 hr
.
•
28
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found L/H MLG Strut placard to be worn.
Est 1 hr, $75 parts
29
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found L/H MLG wheel well A/C ducting to have signs of surface corrosion
near the gama coupling attach clamps.
Est 4 hr
30
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found L/H MLG follow up door, main door and landings to have minor
chaffing.
Est 4 hr
31
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found both L/H MLG and R/H MLG wheel wells to be dirty.
-Info only, 8 hrs to clean if desired-
32
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG follow up door, main door and landings to have minor
chaffing.
Est 4 hr
33
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG wheel well aft inboard flange corroded with evidence of
blue water staining.
Est 40 hr, parts tbd
34
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG Door aft upper corner to be corroded with evidence of blue
water staining.
Est 40 hr, parts tbd
35
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG wheel well aft wall where the composite structure meets an
aluminum stiffener to be corroded.
Est 10 hr
36
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection R/H MLG wheel well A/C ducting to have signs of surface corrosion near the
gama coupling attach clamps.
Est 6 hr
37
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
Trunnion L/H mount pin to be incorrectly installed. (Per GIV MM 32-24-01 the
lubrication fitting should be below center line)
Est 4 hrs
Report Date: << DRAFT as of xx./xx/xxxx >>
Page 3 of x
EFTA00802481
Aircraft Records & Condition Survey
GIV SIN 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Gulfstreard
it•assnat
'arra...rat
all••••••
Id V
Report Date: « DRAFT as of xxhochootx »
Page 4 of x
EFTA00802482
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Gill fist n itt&
•••••1••••••I
NA EWA,. 4.4.1a40AMV
38
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
Wheel well hydraulic phenolic block to be missing a fastener.
Est 2 hrs
39
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
Wheel well on the R/H side to have Hydraulic line that shows signs of leaking.
Est 2 hrs
40
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
Wheel well Accumulator Plexiglas protective cover to be cracked.
Est 1 hr, parts $250
41
The following CMP codes are due before the proposed aircraft release date: 237004,
240262, 320004, 320005, 320006, and 322042
42
While complying with CMP 534020 Nose Wheel Well and Gear — Inspection found NLG
RH door to have small area of corrosion.
Est 2 hr
43
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG Shock strut placard to be worn.
Est 1 hr, parts $75
44
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found MLG Torque Box Shelf to have multiple hydraulic feed through at
aluminum brackets to show signs of surface corrosion.
Est 4 hr, parts TBD
45
While Complying with CMP 534018 Main Landing Gear Wheel Well Compartment -
Inspection found R/H MLG Follow up door to have multiple spots of surface corrosion
that will require further evaluation.
Est 10 hrs
46
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
follow up door link rods to have excessive play.
Est 2 hrs, parts $200
47
While Complying with CMP 534020 Nose Wheel Well and Gear - Inspection found NLG
follow up door to have excessive play at fuselage hinge.
Est 14 hrs, parts $200
48
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found elevator trim cable turnbuckle safety clips are not locked.
49
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found bent landing on left and right side of tail compartment door cutout.
Est 2 hrs
50
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found floorboard (FLR-64) is bowed in throughout most of the surface and core is
crushed.
Est 10 hrs, parts $1000
51
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found flight hydraulic filter manifold is wet with Skydrol at upper cap.
Est 2 hrs
Report Date: << DRAFT as of xx./xxJxxxx >>
Page 5 of x
EFTA00802483
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Gt 11 fist Hearn'
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n
4.M...ft...I
52
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found hydraulic fluid spillage and bubbled paint on structure below utility pump.
Est 2 hrs
53
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found APU bleed air duct fire seal clamp is missing.
Est 1 hr, parts $15
54
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found wire harness tie-down is disbonded from the pressure bulkhead beam lightning
hole.
Est 1 hr
55
While complying with GIV CMP 532067 - Tail Compartment Above Floor - Inspection,
found rudder actuator is wet with hydraulic fluid.
Est 2 hr
56
While performing ARCS hot cockpit / cabin inspection noted source switching on cabin
VIP Switch Panel will cycle thru DVD 1 and 2 but does not display video to the
monitor. DVD will play, as we were able to get sound playing thru the sound system for
the DVD
Est TBD
S7
While performing ARCS hot cockpit / cabin inspection noted Custom Bose surround
sound system will not play aft cabin audio when attempting to play DVD audio. System
will play correctly with iPod selected
Est TBD
58
While performing ARCS hot cockpit / cabin inspection noted All the headphone switch
panels do not work. When plugged in and turning the volume to max, you can hear the
cycling of audio sources but none of the iPod/DVD audio came thru
Est TBD
59
While performing ARCS hot cockpit / cabin inspection noted RH Window No. 5 and LH
Window No. 1 upwash lights are inop
Est 3 hrs, parts $320
60
While performing ARCS hot cockpit / cabin inspection noted Left Seat No. 1 has a
switch that says seat window shade, upon activating said switch it controls all the
shades.
Est TBD
61
While performing ARCS hot cockpit / cabin inspection noted RH Seat No. 2 VIP switch
panel will consistently override whatever action you are trying to make to show cabin
temp. For example, when trying to cycle thru Video sources after every selection the
cabin temp would display
Est TBD
62
While performing ARCS hot cockpit / cabin inspection noted All the 60Hz outlets had
polarity reversed but seem to function as advertised
Est TBD
63
While performing ARCS hot cockpit / cabin inspection noted The cabin remote that is
docked at the VIP seat would only control certain functions. For example, it would
eject the DVD from the player, but when attempting to select the FWD Monitor source,
nothing would happen
Est TBD
64
While complying with CMP 534018 Main landing gear wheel well compartment
inspection found MLG torque box surface to show signs of corrosion that will require
further evaluation.
Est 10 hrs
Report Date: << DRAFT as of xxixrJxxxx >>
Page 6 of x
EFTA00802484
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
( it ilfst mutt&
••••••1.4.4.•
•••••
4 4•••••••••,/
65
While C/W CMP 571005 Wing Exterior (Left) Inspection found sealant missing on
leading edge gap bands.
Est 1 hr
66
While C/W CMP 571005 Wing Exterior (Left) Inspection found all flap tracks to have
rust/corrosion where rollers contact the track.
Est 40 hrs, parts TBD
67
While C/W CMP 571005 Wing Exterior (Left) Inspection found wing to flap seal
between inboard and second flap track on wing trailing edge to be torn.
Est 1 hr
68
While C/W CMP 571006 Wing Exterior (Right) Inspection found wing to flap seal
between second and third flap track on wing trailing edge to be torn.
Est 1 hr
69
While C/W CMP 571006 Wing Exterior (Right) Inspection found all flap tracks to have
rust/corrosion where rollers contact the track.
Est 40 hrs, parts TBD
70
While C/W CMP 571006 Wing Exterior (Right) Inspection found right wing navigation
light lens to have major crazing/cracking.
Est 6 hrs, parts $1200
71
While C/W CMP 532005 Cabin Compartment Above Floor Inspection found cabin
upwash light over right fwd emergency exit to be out.
-NA DUPLICATE-
72
While C/W CMP 532005 Cabin Compartment Above Floor Inspection found cabin
downwash light between right emergency exits and last right cabin downwash light to
be out.
73
While C/W CMP 532027 Entrance Compartment Behind Panel Inspection, found engine
synchronizer amplifier/control box to be missing one of four screws securing it to the
cabinet.
Est 1 hr
74
While C/W CMP 533005 Exterior Fuselage Inspection, noted skeg paint is worn down to
bare metal around fwd drain hole.
Est 1 hr
75
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H A track
flap trough to show signs of surface corrosion that will require further evaluation.
Est 3 hrs
76
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H A track
flap trough roller to be corroded.
Est 3 hrs, parts $150
77
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H B track
flap trough roller to be seized.
Est 3 hrs, parts $150
78
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H B track
Aft outboard small roller to be worn.
Est 1 hrs, parts $50
79
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H C track
flap trough roller to be corroded.
Est 3 hrs, parts $150
Report Date: << DRAFT as of xx/xxfxxxx >>
Page 7 of x
EFTA00802485
Aircraft Records & Condition Survey
GIV S/N 1085 N120JE
ACTT: 9801.3 ACTL: 4451
ARCS Performed By:
Git first ira.rns
•
I
I IniNa•••••
4 41.0.....afre
80
While complying with CMP 571006 Wing Exterior (Right) - Inspection found R/H D track
Roller rub strips to be worn beyond limits.
Est 1 hr, parts $50
81
While complying with CMP 571005 Wing Exterior (Left) - Inspection found L/H A track
flap trough roller to be corroded.
Est 3 hrs, parts $150
82
While complying with CMP 571005 Wing Exterior (Left) - Inspection found L/H B track
aft inboard small roller worn.
Est 1 hrs, parts $50
83
While complying with CMP 571005 Wing Exterior (left) - Inspection found L/H C track
aft outboard small roller worn.
Est 1 hrs, parts $50
84
While complying with CMP 571005 Wing Exterior (left) - Inspection found L/H C track
flap trough roller to be corroded.
Est 3 hrs, parts $150
85
While complying with CMP 571005 Wing Exterior (Left) - Inspection found L/H D track
Roller rub strips to be worn beyond limits.
Est 1 hrs, parts $50
86
While complying with CMP 533005 - Exterior Fuselage - Inspection found Co-pilot
windshield to have inter-pane cracking at bus bar.
Est 12 hr, parts $53,150
87
While complying with CMP 533005 - Exterior Fuselage - Inspection found Co-pilot side
window to have inter-pane cracking at bus bar.
Est 12 hr, parts $12,000
88
While complying with GIV CMP 532067 Tail compartment above floor — inspection
noted light coating con of fluid and small misc debris on and within tail compartment FS
596 Junction box.
Est 2 hrs
89
While complying with GIV CMP 532067 tail compartment above floor — inspection
noted failed fastener on tail compartment FS 596 junction box cover.
Est 1 hr
90
During APU operational test noted overspeed test did not test.
Est 4 hrs, parts TBD
91
While complying with CMP 532017 Cockpit compartment above floor inspection, found
pilot side window has long scratches and waviness as well as outer seal deterioration
that will required further investigation.
Est 4 hrs
92
While complying with CMP 532041 baggage compartment inspection found baggage
door to have cracks in the fwd and aft lower radius and fwd upper radius that will
require further evaluation.
Est 30 hrs, parts TBD
Report Date: << DRAFT as of xx./xxJxxxx >>
Page 8 of x
EFTA00802486
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Tail #
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